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CN101126035B - Phenol water closed operation high-conversion coal gasification production technique - Google Patents

Phenol water closed operation high-conversion coal gasification production technique Download PDF

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CN101126035B
CN101126035B CN2007100171594A CN200710017159A CN101126035B CN 101126035 B CN101126035 B CN 101126035B CN 2007100171594 A CN2007100171594 A CN 2007100171594A CN 200710017159 A CN200710017159 A CN 200710017159A CN 101126035 B CN101126035 B CN 101126035B
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刘圣照
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SHANDONG YISHENG ENVIRONMENTAL PROTECTION EQUIPMENT CO Ltd
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Abstract

一种酚水封闭运行高转化率煤气化生产工艺,包括气化剂,其特征是,所述气化剂的温度为65~350℃,含水量为55~60℃时同重量饱和空气的含水量。所述气化剂是含酚废水在压力泵作用下,在混合箱中雾化与热空气充分混合形成的,并在风机作用下,进入气化炉参加反应。本发明的含酚废水是指煤气在冷却过程中析出的含有苯、酚等水溶液,是在气化工艺系统完全封闭的环境中,采用机械方式,被输送到炉体氧化层内得到裂解焚烧,不外排,彻底解决了酚水污染及二次污染问题;部分热量重新回炉利用,节省了参与氧化反应煤的量,从而,气化效率提高3%~5%,气化强度提高10%以上。

Figure 200710017159

A phenolic water closed operation high-conversion coal gasification production process, including a gasification agent, is characterized in that the temperature of the gasification agent is 65-350°C, and the water content is 55-60°C when the same weight of saturated air is water volume. The gasification agent is formed by fully mixing the phenol-containing waste water with the hot air in the mixing box under the action of the pressure pump, and enters the gasification furnace to participate in the reaction under the action of the fan. The phenol-containing waste water of the present invention refers to the aqueous solution containing benzene, phenol, etc. that is separated out during the cooling process of the coal gas. It is transported mechanically to the oxide layer of the furnace body to be cracked and incinerated in a completely closed environment of the gasification process system. No external discharge, completely solve the problem of phenol water pollution and secondary pollution; part of the heat is returned to the furnace for use, saving the amount of coal participating in the oxidation reaction, thus increasing the gasification efficiency by 3% to 5%, and the gasification intensity by more than 10%. .

Figure 200710017159

Description

一种酚水封闭运行高转化率煤气化生产工艺A high-conversion coal gasification production process with closed operation of phenol water

技术领域technical field

本发明属于煤的气化工艺技术领域,具体涉及一种酚水封闭运行高转化率煤气化生产工艺。The invention belongs to the technical field of coal gasification technology, and in particular relates to a coal gasification production technology with high conversion rate in closed operation of phenol water.

背景技术Background technique

如图1所示,传统的两段炉冷媒气生产工艺如下:通过输送机构,将合适质量及大小的煤块送入煤仓,由加煤机构连续并均匀的加入到煤气炉内,在煤气炉内,存在以下三类主要的化学反应:1、煤中的碳与气化剂空气中氧、水蒸汽之间的反应;2、气化剂中的氧、水蒸汽、各种生成气之间的反应;3、煤的热裂解反应,这三种反应在炉内不同层次进行。As shown in Figure 1, the traditional two-stage furnace refrigerant gas production process is as follows: through the conveying mechanism, coal blocks of appropriate quality and size are sent to the coal bunker, and the coal feeding mechanism is continuously and evenly added to the gas furnace. In the furnace, there are the following three main chemical reactions: 1. The reaction between the carbon in the coal and the oxygen and water vapor in the air of the gasification agent; 2. The reaction between the oxygen, water vapor in the gasification agent, and various generated gases 3. Coal pyrolysis reaction, these three reactions are carried out at different levels in the furnace.

氧化层又成为火层,正常情况下厚度为100~200mm。氧化层主要的作用是使空气中的氧气遇炭进行急剧的热化学反应,生成大量的二氧化碳,同时放出热量。煤气的热化学反应所需的热量靠此来维持。火层温度一般保持在1100~1250℃,决定于原料煤灰熔点的高低。The oxide layer becomes the fire layer again, and the thickness is 100-200mm under normal circumstances. The main function of the oxide layer is to make the oxygen in the air meet with carbon to undergo a rapid thermochemical reaction, generate a large amount of carbon dioxide, and release heat at the same time. The heat required for the thermochemical reaction of the gas is maintained by this. The temperature of the fire layer is generally maintained at 1100-1250°C, which depends on the melting point of the raw coal ash.

还原层是生成主要可燃气体的区域,根据反应式进行的情况,分为第一还原层和第二还原层(或成为主还原层和次还原层)。正常情况下,还原层厚度为200~400mm。还原层的作用是:①二氧化碳和灼热的炭起作用,进行热化学反应,生成可燃的一氧化碳;②水蒸汽与灼热的炭进行吸热化学反应,生成可燃的一氧化碳和氢气;③除以上两类反应外,其次还有一氧化碳与多余的水蒸汽反应而生产二氧化碳和氢气,同时放出热量。The reduction layer is the area where the main combustible gas is generated, and is divided into the first reduction layer and the second reduction layer (or the main reduction layer and the second reduction layer) according to the progress of the reaction formula. Under normal circumstances, the thickness of the reduction layer is 200-400mm. The role of the reduction layer is: ① carbon dioxide and hot charcoal act together to perform a thermochemical reaction to generate combustible carbon monoxide; ② water vapor and hot charcoal undergo an endothermic chemical reaction to generate combustible carbon monoxide and hydrogen; ③ except for the above two types In addition to the reaction, carbon monoxide reacts with excess water vapor to produce carbon dioxide and hydrogen, while releasing heat.

两段式发生炉煤气分上下两段,上段煤气由发生炉顶部出口离去,进入电捕焦油器除去焦油,焦油流入焦油罐。夹套内的冷却水通过蒸汽管进入蒸汽包。产生的煤气进入间冷器,经冷却后由底部离去,煤气被冷却后冷凝析出有毒酚水由水管流入酚水池;煤气进入电除焦油器除去轻油,轻油流入储油罐,净化后的煤气借煤气排送机送往用户。The gas in the two-stage generator is divided into upper and lower stages. The gas in the upper stage leaves from the top outlet of the generator and enters the electric tar catcher to remove tar, and the tar flows into the tar tank. The cooling water in the jacket enters the steam drum through the steam pipe. The generated gas enters the intercooler and leaves from the bottom after being cooled. After the gas is cooled, it condenses and precipitates toxic phenol water, which flows into the phenol pool through the water pipe; the gas enters the electric detarter to remove light oil, and the light oil flows into the oil storage tank. After purification The gas is sent to the user by the gas delivery machine.

混合发生炉煤气是采用空气和水蒸气混合气作为气化剂,在发生炉内与碳进行气化反应生成可燃气体。水蒸气的作用如下:Mixed producer gas uses the mixture of air and steam as the gasification agent, and reacts with carbon in the producer to generate combustible gas. The effect of water vapor is as follows:

(1)由于水蒸气分解吸收热量,因而可降低炉内温度。水量的多少是通过控制气化剂饱和温度来控制水量。(1) Since the water vapor decomposes and absorbs heat, the temperature in the furnace can be reduced. The amount of water is controlled by controlling the saturation temperature of the gasifying agent.

(2)由于水蒸气能降低炉温,所以减弱了二氧化碳遇碳还原为一氧化碳的反应速度,使一氧化碳与二氧化碳的比值降低。(2) Since water vapor can lower the furnace temperature, the reaction rate of reducing carbon dioxide to carbon monoxide when it encounters carbon is weakened, so that the ratio of carbon monoxide to carbon dioxide is reduced.

(3)由于水蒸气在适当炉内温度条件下,大部分可分解生成氢气和一氧化碳,所以提高了煤气的质量,使煤气发热值增加。(3) Since most of the water vapor can be decomposed to generate hydrogen and carbon monoxide under appropriate furnace temperature conditions, the quality of the gas is improved and the calorific value of the gas is increased.

(4)水蒸气不能完全分解,分解率的大小与炉内温度、煤炭性质、水蒸气量的多少等因素有关。未分解的水蒸气均混入煤气中,并流出发生炉。这样由于煤气炉出温度较高,使热损失增加,同时煤气中带水分多时,需净化冷却,否则会影响管路寿命及用户的使用,由于煤气降温,在管道中排水量较多,严重时妨碍正常送气,并降低了用户加热设备的热效率。(4) Water vapor cannot be completely decomposed, and the decomposition rate is related to factors such as the temperature in the furnace, the nature of the coal, and the amount of water vapor. Undecomposed water vapor is mixed into the gas and flows out of the generator. In this way, due to the high temperature of the gas furnace, the heat loss increases. At the same time, when there is a lot of water in the gas, it needs to be purified and cooled, otherwise it will affect the life of the pipeline and the use of users. Air supply is normal, and the thermal efficiency of the user's heating equipment is reduced.

由于上述原因,水蒸气对煤气生产的正常、操作的难易、煤气的质量以及生产过程的经济性均有影响。目前,气化剂中的水蒸气量均采用混合气体的饱和温度来控制,例如,某混合煤气站气化剂采用空气水蒸汽的混合气,水量的大小是55~60℃的饱和蒸汽所含有的水量,水量的控制是在空气和水蒸汽同时输运到混合箱内,利用温控感应器,通过控制混合汽的温度,达到自动调整水蒸汽的进量。《职业技术》2006年第10期第152页《煤气发生炉气化过程分析》(杨立森、王帝文)公开了一般鼓风温度范围在50~65℃,其公开的内容在此引用。Due to the above reasons, water vapor has an impact on the normality of gas production, the ease of operation, the quality of gas and the economy of the production process. At present, the amount of water vapor in the gasification agent is controlled by the saturation temperature of the mixed gas. For example, the gasification agent of a mixed gas station uses a mixture of air and water vapor. The water volume is controlled by transporting air and water vapor into the mixing box at the same time, and using the temperature control sensor to automatically adjust the water vapor intake by controlling the temperature of the mixed steam. "Professional Technology" No. 10, 2006, page 152 "Analysis of Gasification Process of Coal Gasifier" (Yang Lisen, Wang Diwen) discloses that the general blast temperature ranges from 50 to 65°C, and the disclosed content is quoted here.

这种采用饱和蒸汽法,有诸多的优点,技术含量要求低,利用循环冷却水产生的蒸汽进入炉内,操作简便,易于控制,监控点相对较少。This method of using saturated steam has many advantages, low technical content requirements, using the steam generated by circulating cooling water to enter the furnace, easy to operate, easy to control, and relatively few monitoring points.

煤气生产过程中污水产生的原因:Causes of sewage generated during gas production:

煤气站的含酚污水主要含有焦油、轻油、粗酚、氨和硫等五种污染物质(煤气水成分在不同的装置中略有差异),其中酚类以一元酚为主,以苯酚含量最高,其次还有间对甲苯酚,其来源于冷却及净化煤气过程中的洗涤水和含酚冷凝水,其中含酚冷凝水的生成量取决于气化煤质及所采用的气化工艺。以两段炉煤气站气化大同烟煤为例,上段煤气经间接冷却器最终冷却,产生的冷凝水量约为100kg/t煤左右,该冷凝水含酚量约为8500~10000mg/L;下段煤气洗涤水含酚量10mg/L,而且冷凝水随着循环使用时间的增加,其含酚量也不断地增加,增加到一定程度后,便会影响洗涤冷却设备中的传质与换热,从而带来一系列不良影响。The phenol-containing sewage of the gas station mainly contains five kinds of pollutants such as tar, light oil, crude phenol, ammonia and sulfur (the composition of gas water is slightly different in different devices), among which the phenols are mainly monohydric phenols, and the content of phenol is the highest , followed by m-p-cresol, which comes from the washing water and phenol-containing condensate in the process of cooling and purifying the gas. The amount of phenol-containing condensate depends on the gasification coal quality and the gasification process used. Taking the gasification of Datong bituminous coal in the two-stage furnace gas station as an example, the gas in the upper stage is finally cooled by the indirect cooler, and the condensed water produced is about 100kg/t coal, and the phenol content in the condensed water is about 8500-10000mg/L; the gas in the lower stage The phenol content of the washing water is 10mg/L, and the phenol content of the condensed water increases continuously with the increase of the cycle time. After increasing to a certain extent, it will affect the mass transfer and heat exchange in the washing and cooling equipment, thus bring a series of adverse effects.

几十年来,如何彻底治理含酚污水一直是困扰煤气站的环保难题,从事工业煤气设计研究的专家们经过长期的研究与探讨,虽然摸索到了一些行之有效的处理方法,也取得了一定的效果,但是仍存在诸多不足之处。For decades, how to thoroughly treat phenol-containing sewage has been an environmental problem that plagues gas stations. After long-term research and discussion, experts engaged in industrial gas design and research have found some effective treatment methods and achieved certain results. effect, but there are still many shortcomings.

含酚污水的几种常规处理方法:Several conventional treatment methods for phenolic sewage:

对于煤气站的含酚污水处理一般分为两个阶段:第一,预处理阶段,该阶段旨在除去污水中的大部分悬浮物及焦油等;第二,脱酚处理阶段,其目的是将预处理后的污水中的大部分 酚类物质及部分有机物质脱除。The treatment of phenol-containing sewage in gas stations is generally divided into two stages: first, the pretreatment stage, which aims to remove most of the suspended solids and tar in the sewage; second, the dephenol treatment stage, whose purpose is to remove Most of the phenolic substances and some organic substances in the pretreated sewage are removed.

1.1预处理方法:在煤气站中已经应用的预处理方法,目前一般有以下几种:1.1 Pretreatment methods: The pretreatment methods that have been applied in gas stations generally include the following:

1)自然沉降分离法;2)机械过滤法;3)化学混凝沉淀法;4)电解浮选法;5)离心分离法;6)加酸破乳焦油渣吸附法;7)加压溶气气浮法;8)射流气浮法1) natural sedimentation separation method; 2) mechanical filtration method; 3) chemical coagulation precipitation method; 4) electrolytic flotation method; 5) centrifugal separation method; Air flotation method; 8) jet air flotation method

其中自然沉降分离法,可直接设置在煤气站的循环水工艺系统中,虽然效果不是十分理想,但运行成本较低,一直被大多数煤气站作为含酚污水预处理方法所采用。其它七种方法则必须在另行设置的设备中进行处理,相对处理费用要高出许多。Among them, the natural sedimentation separation method can be directly installed in the circulating water process system of the gas station. Although the effect is not very ideal, but the operation cost is low, and it has been adopted by most gas stations as a pretreatment method for phenolic sewage. The other seven methods must be processed in additional equipment, and the relative processing costs will be much higher.

1.2脱酚处理方法:脱酚处理方法可分为物理化学法和生物化学法。1.2 Dephenolization treatment method: The dephenolization treatment method can be divided into physical chemical method and biochemical method.

1.2.1物理化学法1.2.1 Physicochemical method

1.2.1.1蒸汽化学脱酚法1.2.1.1 Steam chemical dephenolization method

用强烈的高温蒸汽加热含酚污水,使污水中的酚蒸发后随蒸汽逸出,然后再通入碱液吸收成为酚钠盐,从而达到脱酚的目的。该法操作简单,投资也较少,但蒸汽耗量较大,且脱酚效率不够理想,一般达不到彻底治理之目的。Use strong high-temperature steam to heat phenol-containing sewage, so that the phenol in the sewage evaporates and escapes with the steam, and then passes through the lye to absorb and become phenol sodium salt, so as to achieve the purpose of dephenolization. This method is simple to operate and requires less investment, but the steam consumption is relatively large, and the dephenolization efficiency is not ideal, and the purpose of thorough treatment is generally not achieved.

1.2.1.2蒸汽脱酚法1.2.1.2 Steam dephenolization method

将含酚污水加热,使酚随水蒸汽挥发出来,再将这部分含酚蒸汽通入发生炉炉底混入空气中作为气化剂使用,在炉内,酚在高温下燃烧分解成CO2和H2O最终达到脱酚的目的。其缺点在于此法只能脱除低沸点酚系物,且能耗较大,每蒸发1吨污水约需燃料折合标煤180公斤左右,其缺点是此法处理含酚污水,能耗大且煤气炉炉底饱和温度不易控制。Heat the phenol-containing sewage to volatilize the phenol with the water vapor, and then pass this part of the phenol-containing steam into the bottom of the generator furnace and mix it with air as a gasification agent. In the furnace, the phenol is burned and decomposed into CO2 and H 2 O finally achieves the purpose of dephenolization. The disadvantage is that this method can only remove low-boiling point phenols, and the energy consumption is relatively large. It takes about 180 kilograms of fuel equivalent to standard coal to evaporate 1 ton of sewage. The saturation temperature of the bottom of the gas furnace is not easy to control.

1.2.1.3焚烧法1.2.1.3 Incineration method

将含酚污水喷入焚烧炉,使酚类有机物在1100℃左右的高温下,发生氧化反应,最终生成CO2和H2O排放,此法工艺简单,操作方便,但能耗较大,每焚烧1吨含酚废水其成本约在200元左右。上一世纪90年代初期,国外引进的及国内配套的两段式煤气发生炉基本上都配备有酚水焚烧炉设施,但基本上都因能耗问题而闲置不用。利用焚烧法处理含酚污水另一个关键缺点在于一旦操作不慎,炉温下降,往往会造成燃烧不完全,易形成二次污染。The phenolic sewage is sprayed into the incinerator, so that the phenolic organic matter will undergo oxidation reaction at a high temperature of about 1100 ° C, and finally generate CO 2 and H 2 O emissions. This method has a simple process and is easy to operate, but it consumes a lot of energy. The cost of incinerating 1 ton of phenolic wastewater is about 200 yuan. In the early 1990s, the two-stage gasifiers imported from abroad and domestically supported were basically equipped with phenol water incinerator facilities, but they were basically idle due to energy consumption problems. Another key disadvantage of using incineration to treat phenol-containing sewage is that once the operation is careless, the furnace temperature will drop, which will often cause incomplete combustion and easily form secondary pollution.

1.2.1.4溶剂萃取脱酚法1.2.1.4 Solvent extraction dephenolization method

该法的主工艺分萃取和解吸两部分,萃取过程是一个物质再分配过程,利用萃取剂将酚从污水中萃取出来;含酚萃取剂再与碱液相互接触,萃取剂中的酚与碱发生反应生成酚钠盐,该过程是一个解吸过程。利用该种脱酚方法处理后的出水尚含100-200mg/l的酚,不能直接 排放,而且萃取剂的流失会造成污水乳化,并形成二次污染。另外该方法须采用高效率的萃取剂及碱,运行成本较高。The main process of this method is divided into two parts: extraction and desorption. The extraction process is a material redistribution process. The phenol is extracted from the sewage by using the extractant; A reaction occurs to generate sodium phenolate, which is a desorption process. The effluent treated by this kind of phenol removal method still contains 100-200mg/l phenol, which cannot be discharged directly, and the loss of the extractant will cause the emulsification of sewage and form secondary pollution. In addition, this method must use high-efficiency extractant and alkali, and the operating cost is relatively high.

1.2.1.5树脂脱酚法1.2.1.5 Resin dephenolization method

该法主要工艺过程包括吸附和解吸,用树脂吸附废水中的酚,然后用碱液进行解吸,生成酚钠,此法工艺过程较为复杂,且影响脱酚效率的因素较多,运行成本相对较高。The main process of this method includes adsorption and desorption. The phenol in the wastewater is adsorbed by resin, and then desorbed by lye to generate sodium phenate. The process of this method is relatively complicated, and there are many factors affecting the efficiency of phenol removal, and the operating cost is relatively high. high.

1.2.1.6磺化煤吸附法1.2.1.6 Sulfonated coal adsorption method

该法以磺化煤极性基团吸附酚,然后以碱液吸收而成酚钠盐脱酚,磺化煤吸附是间歇进行的,完成一次循环包括吸附和再生两个环节。该法的主要缺点在于磺化煤的吸酚量过低,吸附周期太短,解析、再生也比较困难。In this method, phenol is adsorbed by sulfonated coal polar groups, and then absorbed by lye to form phenol sodium salt for dephenolation. The adsorption of sulfonated coal is carried out intermittently, and one cycle includes two links of adsorption and regeneration. The main disadvantage of this method is that the amount of phenol absorbed by sulfonated coal is too low, the adsorption period is too short, and it is difficult to analyze and regenerate.

1.2.1.7生化法1.2.1.7 Biochemical method

对含酚污水进行生化处理是培养微生物,并利用微生物将污水中的酚类有机物消化吸收分解成H2O和CO2的过程。该方法根据微生物的承载方式及供氧方式的不同又可分为曝气法、接触氧化法、生物转盘法及生物滤池法等。生化法对进入生化池的污水水质要求较为严格,污水中焦油及酚等有机物浓度不可超过微生物所能承受的浓度,否则,需要将污水稀释后才能进入生化池,这样便限制了处理水量。同时微生物驯化比较困难,进水浓度超标、环境温度不适宜,都很容易限制微生物的生存。东北某厂曾采用生化法处理含酚污水,由于条件要求严格致使其处理成本相当高。Biochemical treatment of phenolic sewage is a process of cultivating microorganisms and using microorganisms to digest, absorb and decompose phenolic organic matter in sewage into H 2 O and CO 2 . This method can be divided into aeration method, contact oxidation method, biological turntable method and biological filter method according to the different ways of carrying microorganisms and oxygen supply. The biochemical method has strict requirements on the quality of the sewage entering the biochemical pool. The concentration of organic matter such as tar and phenol in the sewage should not exceed the concentration that microorganisms can withstand. Otherwise, the sewage needs to be diluted before entering the biochemical pool, which limits the amount of treated water. At the same time, it is difficult for microorganisms to domesticate. The concentration of influent water exceeds the standard and the ambient temperature is not suitable, which can easily limit the survival of microorganisms. A factory in Northeast China used biochemical methods to treat phenolic wastewater, but the cost of treatment was quite high due to strict requirements.

纵上所述,无论是焚烧还是生化法,要么成本高要么造成二次污染,在目前众多的煤气站中,酚水处理非常理想的用户极为少见。As mentioned above, whether it is incineration or biochemical method, either the cost is high or secondary pollution is caused. Among the many gas stations at present, there are very few users who are very ideal for phenol water treatment.

公开号为CN1162624A的中国专利公开了一种两段炉水煤气厂工艺流程与含酚水的处理,包括气化、冷却净化和含酚水处理工艺,其中,含酚水处理部分是由含酚水泵、燃烧蓄热器、两段炉组成,含酚水是利用空气吹风气的能量,将燃烧蓄热器内的格子砖烧到800~900℃高温,然后在下制气时把含酚水喷入燃烧蓄热器内,与格子砖进行热交换而气化,然后作为气化剂进入两段炉内与炽热的焦炭产生水煤气的过程把含酚水处理掉。The Chinese patent with the publication number CN1162624A discloses a two-stage furnace water gas plant process flow and the treatment of phenol-containing water, including gasification, cooling and purification, and phenol-containing water treatment processes, wherein the phenol-containing water treatment part is provided by a phenol-containing water pump. , combustion regenerator, and two-stage furnace. The phenol-containing water uses the energy of air blowing to burn the checker bricks in the combustion regenerator to a high temperature of 800-900°C, and then sprays the phenol-containing water into the In the heat accumulator, it is gasified by heat exchange with checker bricks, and then enters the two-stage furnace as a gasification agent to produce water gas with hot coke to dispose of the phenolic water.

发明内容Contents of the invention

本发明针对现有技术中存在的不足,从煤气发生氧化与还原反应需要的热平衡入手,采用炉内焚烧酚水而不外排,使得煤气酚水在完全封闭的条件下运行,有效的避免了环境污染问题,并且,由于有效的利用了煤气余热以及酚燃烧产生的热量,因而,煤转化成煤气的气化率和煤气炉炉体单位面积的气化强度都有了提高。The present invention aims at the deficiencies in the prior art, starting from the heat balance required for the oxidation and reduction reactions of the gas, and adopts the method of incinerating the phenol water in the furnace without discharging it, so that the gas phenol water operates under a completely closed condition, effectively avoiding the Environmental pollution problems, and, due to the effective use of gas waste heat and the heat generated by phenol combustion, the gasification rate of coal into gas and the gasification intensity per unit area of the gas furnace body have been improved.

本发明具体采用如下技术方案:The present invention specifically adopts the following technical solutions:

一种酚水封闭运行高转化率煤气化生产工艺,包括气化剂,其特征是,所述的气化剂的温度大于65℃,含水量为55~60℃时同重量饱和空气的含水量。A phenol water closed operation high-conversion coal gasification production process, including a gasification agent, characterized in that the temperature of the gasification agent is greater than 65°C, and the water content is the same weight of saturated air when the water content is 55-60°C .

所述的气化剂的温度为65~80℃、80~150℃或者150~250℃。The temperature of the gasifying agent is 65-80°C, 80-150°C or 150-250°C.

所述的气化剂是含酚水在混合箱中雾化并与热空气混合后制得,下一步进入两段炉;所述的热空气是空气在风冷器、废热锅炉或者输气管道中进行热交换后温度为300~500℃的空气,下一步进入混合箱。The gasifying agent is made by atomizing phenol-containing water in a mixing box and mixing it with hot air, and then enters the two-stage furnace in the next step; The air with a temperature of 300-500°C after heat exchange in the middle enters the mixing box in the next step.

本发明的有益效果在于:与传统的煤气炉制气工艺相比,进入炉底的空气在换热设备中与高温煤气发生了热交换,变成高温空气,在鼓风机的作用下,被送入混合箱中,酚水被酚水泵输送到混合箱中,在混合箱中有雾化装置,雾化装置将酚水雾化后,在高温空气中发生闪蒸现象,被迅速气化,气化剂是不饱和的热空气,进入炉底的相对湿度较小,而传统的工艺中,常温空气中加入热蒸汽,进入炉前变成了过饱和的空气,将有部分水从气态变成液态,进入炉底后需要重新吸收大量的热量气化,对炉底灰层和燃烧层造成一定程度的不利影响,降低了煤气的热值。The beneficial effects of the present invention are: compared with the traditional gas furnace gas production process, the air entering the bottom of the furnace undergoes heat exchange with high-temperature gas in the heat exchange equipment, becomes high-temperature air, and is sent into the In the mixing tank, the phenol water is transported into the mixing tank by the phenol water pump. There is an atomizing device in the mixing tank. After the atomizing device atomizes the phenol water, flash evaporation occurs in the high-temperature air, and it is rapidly vaporized. The agent is unsaturated hot air, and the relative humidity entering the bottom of the furnace is small. In the traditional process, hot steam is added to the air at room temperature, and it becomes supersaturated air before entering the furnace, and part of the water changes from gaseous state to liquid state. , After entering the bottom of the furnace, it needs to absorb a large amount of heat to gasify again, which will cause a certain degree of adverse effects on the ash layer and combustion layer at the bottom of the furnace, and reduce the calorific value of the gas.

本工艺中,含酚废水在完全封闭的环境中运行,在炉体氧化层内得到裂解焚烧,无污染;部分热量重新回炉利用,节省了参与氧化反应煤的量,保证更多的煤参加还原反应,气化效率从而提高3%~5%,气化强度提高10%以上,从间冷器冷凝下来的酚水在完全封闭的环境中被采用机械的方式全部返回到炉膛内焚烧,彻底解决了酚水污染和二次污染的问题。In this process, the phenol-containing wastewater operates in a completely closed environment, and is cracked and incinerated in the oxide layer of the furnace body without pollution; part of the heat is returned to the furnace for use, which saves the amount of coal participating in the oxidation reaction and ensures that more coal participates in the reduction reaction, the gasification efficiency is increased by 3% to 5%, and the gasification intensity is increased by more than 10%. Solved the problems of phenol water pollution and secondary pollution.

本发明煤的转化率高:以热值27000kJ/Kg的晋城煤为例,气化效率76%,一公斤煤浪费掉的热量为6480kJ,若将下段煤气从500℃冷却到200℃的热量回收入炉,热量值约有1200kJ,占一公斤煤总热量的4.4%,占一公斤煤浪费掉热量的18.5%,由于工艺是连续的,能量在连续回收利用的过程中,气化强度得到提高,提高的数值,从理论上可达76(1+0.04)%=92%。The coal conversion rate of the present invention is high: taking Jincheng coal with a calorific value of 27000kJ/Kg as an example, the gasification efficiency is 76%, and the heat wasted by one kilogram of coal is 6480kJ. Income into the furnace, the heat value is about 1200kJ, accounting for 4.4% of the total heat of one kilogram of coal, accounting for 18.5% of the heat wasted by one kilogram of coal, because the process is continuous, the gasification intensity is improved in the process of continuous energy recovery and utilization , the improved value can reach 76 (1+0.04) %=92% theoretically.

附图说明Description of drawings

图1是现有技术煤气化生产工艺流程图;Fig. 1 is a prior art coal gasification production process flow chart;

图2是本发明煤气化生产工艺流程图;Fig. 2 is a flow chart of the coal gasification production process of the present invention;

图3是实施例1的设备流程图;Fig. 3 is the equipment flowchart of embodiment 1;

图4是实施例2的设备流程图Fig. 4 is the equipment flowchart of embodiment 2

图5是实施例3的设备流程图Fig. 5 is the equipment flowchart of embodiment 3

图中,1-煤气炉;2-上段煤气;3-下段煤气;4-旋风收尘器;5-电捕焦油器;6-间冷器; 7-电捕轻油器;8-煤气输出管;9-酚水池;10-热交换器;11-废热锅炉;12-热风机;13-混合箱;14-喷雾装置;15-蒸汽包;16-风冷器;17为热交换器。In the figure, 1-gas furnace; 2-upper gas; 3-lower gas; 4-cyclone dust collector; 5-electric tar catcher; 6-intercooler; 7-electric light oil catcher; 8-gas output 9-phenol pool; 10-heat exchanger; 11-waste heat boiler; 12-hot air blower; 13-mixing box; 14-spray device; 15-steam drum; 16-air cooler; 17 is heat exchanger.

实施例1:空气在风冷器中进行热交换后进入混合箱。Example 1: The air enters the mixing box after heat exchange in the air cooler.

下段煤气3由发生炉体1中上部出口排去,首先,经过旋风除尘器4除掉其中的大部分粉尘,进入废热锅炉11,在废热锅炉11内,高温(550~600℃)煤气与软化水进行热交换,将部分水气化送入蒸汽包15,蒸汽包15内的蒸汽可以作系统内的冲洗用,可以向外提高给用户作为他用,经过废热锅炉11的初步降温,煤气进入空气冷却系统热交换器10,在热交换器10中,热交换器10内布置合适数量的列管,热煤气在管内行进,在风机12的作用下,热交换器10的空气进出口之间产生压差,在压力的作用下,空气在管间穿行,通过管壁传导及辐射作用,煤气得到冷却,空气得到加热。被降温的热煤气,并与上段煤气一起会合进入间冷器6得到进一步的冷却,随后,进入电捕轻油器,净化后借煤气排送机8送往用户。The gas 3 in the lower section is discharged from the outlet of the middle and upper part of the generator body 1. First, most of the dust in it is removed by the cyclone dust collector 4, and enters the waste heat boiler 11. The water performs heat exchange, and part of the water is vaporized and sent to the steam drum 15. The steam in the steam drum 15 can be used for flushing the system, and can be raised outward for other uses by the user. After the initial cooling of the waste heat boiler 11, the gas enters the Air cooling system heat exchanger 10, in the heat exchanger 10, a suitable number of tubes are arranged in the heat exchanger 10, the hot gas travels in the tubes, and under the action of the fan 12, the air between the inlet and outlet of the heat exchanger 10 A pressure difference is generated. Under the action of pressure, the air travels between the tubes, and through the tube wall conduction and radiation, the gas is cooled and the air is heated. The cooled hot gas joins with the upper stage gas and enters the intercooler 6 for further cooling, and then enters the electric light oil capture device, and after purification, it is sent to the user by the gas discharge machine 8.

作为煤气发生炉必须的气化剂——空气,在风机12的抽吸作用下,从热交换器10出口出来时,变成了高温气体(300~500℃)。从间冷器6排出的有毒酚水经酚水泵输送到混合箱13内,在混合箱13内的雾化器14作用下,酚水得到雾化变成小雾滴。气化剂中所需要的水的量一般控制为55~60℃饱和空气的水量,控制加入混合箱内的酚水的量少于这一数值,欠缺的部分通过蒸汽包15内的蒸汽进行弥补。在高温空气的作用下,雾滴在短时间内被迅速蒸发,并通过热风蒸汽管输送到煤气发生炉,控制进入煤气发生炉的空气的温度高于65℃,那么,进入发生炉的空气变成不饱和空气,水处于完全的单分子气体状态,进入炉内经过炉底灰层过程中,不存在气化过程,不会造成灰层温度的大幅降低及偏炉等危害。As the gasification agent necessary for the gasifier—air, under the suction of the blower fan 12, when it comes out from the outlet of the heat exchanger 10, it becomes a high-temperature gas (300-500° C.). The toxic phenolic water discharged from the intercooler 6 is transported into the mixing tank 13 through the phenolic water pump, and under the action of the atomizer 14 in the mixing tank 13, the phenolic water is atomized into small mist droplets. The amount of water required in the gasification agent is generally controlled to be the amount of water saturated with air at 55-60°C, and the amount of phenolic water added to the mixing tank is controlled to be less than this value, and the missing part is made up by the steam in the steam drum 15 . Under the action of high-temperature air, the mist droplets are quickly evaporated in a short period of time, and are transported to the gas generator through the hot air steam pipe, and the temperature of the air entering the gas generator is controlled to be higher than 65°C. Then, the air entering the gas generator becomes Unsaturated air, water is in the state of complete monomolecular gas, and there is no gasification process when entering the furnace and passing through the ash layer at the bottom of the furnace, which will not cause a large decrease in the temperature of the ash layer and damage such as partial furnace.

实施例2:废热锅炉进行热交换工艺。Example 2: The waste heat boiler performs a heat exchange process.

下段煤气3由生炉体1中上部出口排去,首先,经过旋风除尘器4除掉其中的大部分粉尘,进入改型的废热锅炉11,高温(550~600℃)煤气穿过废热锅炉11,内部布置合适数量的列管,热煤气在管内行进,空气自进口进入废热锅炉11,可以在列管的外侧的空隙中穿行,空气出口与炉底相连,在风机12抽吸的作用,空气进出口之间产生压差,在压力的作用下,空气在管见穿行,通过管壁传导及辐射作用,煤气得到冷却,空气得到加热。被降温的热煤气,并与上段煤气一起会合进入间冷器得到进一步的冷却,随后,进入电捕轻油器,净化后借煤气排送机8送往用户。The gas 3 in the lower section is discharged from the upper outlet of the raw furnace body 1. First, most of the dust is removed through the cyclone dust collector 4, and then enters the modified waste heat boiler 11. High temperature (550-600°C) gas passes through the waste heat boiler 11 , an appropriate number of tubes are arranged inside, the hot gas travels in the tubes, the air enters the waste heat boiler 11 from the inlet, and can pass through the outer gap of the tubes, the air outlet is connected to the bottom of the furnace, and the air is sucked by the fan 12. There is a pressure difference between the inlet and outlet. Under the action of the pressure, the air passes through the pipe, and the gas is cooled and the air is heated through the conduction and radiation of the pipe wall. The cooled hot gas joins with the upper stage gas and enters the intercooler for further cooling, and then enters the electric light oil capture device, and after purification, it is sent to the user by the gas discharge machine 8.

从废热锅炉11出来的空气,变成了高温气体(300~500℃),热空气经过热风管、风机12输送到混合箱13内,在混合箱13内雾化器14的作用下,酚水得到雾化变成小雾滴。在高温空气的作用下,雾滴在短时间内被迅速蒸发,并通过热风蒸汽管输送到煤气发生炉。The air from the waste heat boiler 11 becomes a high-temperature gas (300-500° C.), and the hot air is delivered to the mixing box 13 through the hot air pipe and the fan 12. Under the action of the atomizer 14 in the mixing box 13, the phenol The water gets atomized into small mist droplets. Under the action of high-temperature air, the fog droplets are quickly evaporated in a short period of time, and are transported to the gas generator through the hot air steam pipe.

实施例3:输送管进行热交换工艺。Embodiment 3: The heat exchange process is carried out on the conveying pipe.

将煤气输送管进行适当的改造变成换热器17,下段煤气3由发生炉1中部出口排去,经过时输气管时,将热量传给与其逆行的空气,并将其加热。空气出口与风机28相连,在风机的作用下,空气进出口之间产生压差,在压力的作用下,空气与煤气逆行,通过管壁传导及辐射作用,煤气得到冷却,空气得到加热。被降温的热煤气,与上段煤气一起会合进入间冷器得到进一步的冷却,随后,进入电捕轻油器,净化后借煤气排送机13送往用户。从余热锅炉出来的空气,变成了高温气体(300~500℃),热空气经过热风管29、风机28输送到混合箱内,在混合箱内雾化器的作用下,酚水得到雾化变成小雾滴。在高温空气的作用下,雾滴在短时间内被迅速蒸发,并通过热风蒸汽管输送到煤气发生炉。The gas delivery pipe is properly transformed into a heat exchanger 17, and the gas 3 in the lower section is discharged from the middle outlet of the generator 1. When passing through the gas delivery pipe, heat is transferred to the air that is traveling against it, and it is heated. The air outlet is connected to the fan 28, under the action of the fan, a pressure difference is generated between the air inlet and outlet, under the action of the pressure, the air and the gas flow in reverse, through the conduction and radiation of the pipe wall, the gas is cooled and the air is heated. The cooled hot gas joins with the upper stage gas and enters the intercooler for further cooling, and then enters the electric light oil trap, and after purification, it is sent to the user by the gas discharge machine 13. The air from the waste heat boiler becomes high-temperature gas (300-500°C), and the hot air is transported into the mixing box through the hot air pipe 29 and the fan 28. Under the action of the atomizer in the mixing box, the phenol water is mist into small mist droplets. Under the action of high-temperature air, the fog droplets are quickly evaporated in a short period of time, and are transported to the gas generator through the hot air steam pipe.

传统的工艺中,从废热锅炉出来高温的煤气,通过风冷器将多余的热量放散到空气中,被浪费了。本工艺中,将这部分热量重新回炉利用,相对于减少了参如氧化反应的煤的量,有更多的煤参与还原反应,生成有用的煤气,气化率可以提高3%~5%,由于气化剂采用热空气代替室温空气,煤气的气化强度可以提高10%以上,从间冷器冷凝下来的酚水在完全封闭的环境中被采用机械的方式全部返回到炉膛内焚烧,彻底解决了酚水污染和二次污染的问题。In the traditional process, the high-temperature gas from the waste heat boiler is wasted by dissipating excess heat into the air through the air cooler. In this process, this part of the heat is returned to the furnace for utilization. Compared with reducing the amount of coal involved in the oxidation reaction, more coal participates in the reduction reaction to generate useful gas, and the gasification rate can be increased by 3% to 5%. Since the gasification agent uses hot air instead of room temperature air, the gasification intensity of the gas can be increased by more than 10%. The phenol water condensed from the intercooler is mechanically returned to the furnace for incineration in a completely closed environment. Solved the problem of phenol water pollution and secondary pollution.

Claims (4)

1.一种酚水封闭运行高转化率煤气化生产工艺,包括气化剂,其特征是,所述的气化剂的温度为65~250℃,含水量为55~60℃时同重量饱和空气的含水量;所述的气化剂是含酚水在混合箱中雾化并与热空气混合后制得,所述的热空气是空气在风冷器、废热锅炉或者输气管道中进行热交换后温度为300~500℃的热空气。1. A phenolic water closed operation high-conversion coal gasification production process, including a gasification agent, is characterized in that the temperature of the gasification agent is 65 to 250 ° C, and the water content is 55 to 60 ° C when the same weight is saturated Moisture content of the air; the gasification agent is made by atomizing phenol-containing water in a mixing box and mixing with hot air, and the hot air is made by air in an air cooler, waste heat boiler or gas pipeline Hot air with a temperature of 300-500°C after heat exchange. 2.根据权利要求1所述的酚水封闭运行高转化率煤气化生产工艺,其特征是,所述的气化剂的温度为65~80℃。2. The phenol water closed operation high-conversion coal gasification production process according to claim 1, characterized in that the temperature of the gasification agent is 65-80°C. 3.根据权利要求1所述的酚水封闭运行高转化率煤气化生产工艺,其特征是,所述的气化剂的温度为80~150℃。3. The phenol water closed operation high-conversion coal gasification production process according to claim 1, characterized in that the temperature of the gasification agent is 80-150°C. 4.根据权利要求1所述的酚水封闭运行高转化率煤气化生产工艺,其特征是,所述的气化剂的温度为150~250℃。4. The phenol water closed operation high-conversion coal gasification production process according to claim 1, characterized in that the temperature of the gasification agent is 150-250°C.
CN2007100171594A 2007-09-18 2007-09-18 Phenol water closed operation high-conversion coal gasification production technique Expired - Fee Related CN101126035B (en)

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